I got a chance to re-run a pressure test and ran volume tests for the (4) WMI nozzles I have:
Pressure test now reads 200 psi while pump is run. Drops to 150 as soon as pump shuts off though so hard say with certainty what pressure actually is.
Nozzles listed below are all supposedly rated at 100psi. By the math that would mean @200 psi they would flow ~1.5 times rated values. Based on my results tolerance aren’t very tight.
The 3.5, 4, & 5 nozzles were all so close to each other in repeated tests and for the duration they’ll be run I doubt they’re functionally any different. It seems like 4 and 5 are quite undersize. The 3 seems a bit of an over performer and the 10 was pretty close in expectation. Given that in the same system at the same pressure the nozzle rated for 10 gal/hr @100 psi nearly tripled the flow of both the 4 and 5 really highlights how poorly these performed for rating.
3.5 nozzle tested ~4.73 gal/hr (~200psi, 13.8v, 20 oz over 2min)
4.0 nozzle tested ~4.8 gal/hr (~200psi, 13.8v, 20.5 oz over 2min)
5.0 nozzle tested ~5.04 gal/hr (~200psi, 13.8v, 21.3 oz over 2min)
10.0 nozzle tested ~14.27 gal/hr (~200psi, 13.8v 30.42 oz over 1min, due to 1L container used I had to shorten this test)
The pump supply filter was checked to confirm it was clear after the tests. The 5.0 nozzle test was re-run with vent/breather filter removed to ensure it wasn’t limiting flow, though from 10.0 nozzle test it didn’t seem likely. Re-test confirmed early results.
Best yet none of the hoses I made had any leaks during any of the tests! A few joints that weren’t tightened enough did, easy to address. All in all I’m very proud as this was my first time making custom braided ptfe lines. There was some blood involved, but well worth it.
Next step will be to drain the tank entirely, Remove the tank and mounting deck from the ITR for now and continue on getting things I cleaned and in place.
In less fun areas I finally took the time to confirm what I suspected. The upper rear right control/camber arm mount threads were damaged and poorly repaired. Existing repair was too large for regular timesert inserts so I’ve ordered a kit of 10-1.25 bigserts (m14 outer threads) and matching cobalt drill bits to get the holes cleaned out properly.
It looks like the clutch lines shipped and should be delivered Weds?
Also ordered rattle cans of spray max 2k black primer and 2k clear. Plan to scotchbrite the steering column support then see how well the epoxy goes on. Hoping I’ll have enough left to do the evap canister mount and maybe some other miscellaneous brackets. If all goes well I may buy more of the 2k clear to use after a clean up of the headlights.